Lodoga actually has a 8GB storage device.
LodogaSsd variant has a 30GB SSD drive.
However, in boot0 both were mishandled and assigned 4GB for legacy reasons.
Remove the hardcoding of the flash size and let boot0 autodetect the available space.
This commit adds support for changing the default console baud rate configured
within the U-Boot bootloader. That default baud rate is exposed via the value
of the U-Boot 'baudrate' environment variable. This commit removes logic that
hardcoded the console baud rate to 115200 and instead ensures that the U-Boot
'baudrate' variable is always used when constructing the Linux kernel boot
arguments used when booting Sonic.
A change is also made to rc.local to ensure that the specified baud rate is set
correctly in the serial getty service.
#### Why I did it
New PSU could install different type of fan, so fan max/min speed should be read per PSU
#### How I did it
The existing implementation read PSU max/min fan speed from a common file, change it to read from per PSU file
#### How to verify it
Manual test
In order to include the following commits:
d29a49a 2021-08-25 [ACL] Match TCP protocol while matching TCP_FLAG (Azure/sonic-swss#1854)
2569ad9 2021-08-25 Fix sFlow sampling-rate and admin-state (Azure/sonic-swss#1728)
8908a8f 2021-08-19 Change rif_rates.lua and port_rates.lua scripts to calculate rates correct (Azure/sonic-swss#1848)
b42c2fb 2021-08-19 [VS Test] Skip flaky tests (Azure/sonic-swss#1875)
apt-package handling: These are part of the Export variables for .j2 files and is needed for Debian and its derivatives.
How I did it
Add support to slave.mk files to export APT_PACKAGES and DBG_APT_PACKAGES
How to verify it
The apt package, provides the apt management tool, a high-level command-line interface for better interactive usage. APT also includes command-line programs for dealing with packages, which use the library. Three such programs are apt, apt-get and apt-cache and can be verified for their existence.
#### Why I did it
Provide possibility to specify curl options as the present curl support provided in Azure/sonic does not extend capability for options like --user which some of the cisco artifacts are requiring.
#### How I did it
Add extensions to the slave.mk file to include curl options as follows:
$($*_CURL_OPTIONS)
#### How to verify it
Option 1) use curl -u, and environment variables
it with --user <user:password> curl_options. Ex: --user foo:'bar!'
curl -u ${BASIC_AUTH_HEADER} https://foo.bar
This works to obscure password/credential in a terminal session that someone else might see directly or via screen share.
Option 2) Option 1: use curl -n
If you run linux, create a ~/.netrc file and insert your creds there, and use curl -n.
chmod the file to 400. curl knows how to extract your creds from the file silently. You never have to type creds on the command line again.
If you run Windows, and use curl, you must name the file _netrc . As on *nix, the file should be in your home directory, and should have appropriate permissions.
For Administrative APIs , my .netrc file looks like this:
machine foobar-linux
login foo
password bar
Why I did it
Pcied running by python 2.
How I did it
dropped python2 support and add python3 support for pcied in file docker-pmon.supervisord.conf.j2
How to verify it
docker exec pmon supervisorctl status
- Why I did it
New release of MFT has the following changelog / RN
Fixed an issue that resulted in getting MVPD read errors from the mlxfwmanager during fast reboot.
Fixed mlxuptime sometimes generating a time less than previous due the wrong frequency calculation
- How I did it
Update makefile pointer to new version.
- How to verify it
Manually tested on all Mellanox platforms.
*To run VNET route consistency check periodically.
*For any failure, the monit will raise alert based on return code.
Signed-off-by: Volodymyr Samotiy <volodymyrs@nvidia.com>
Fix Chassis.get_name to return the same value than what's in platform.json
Fix Chassis.get_system_eeprom_info when running from within pmon.
Fix Watchdog.get_remaining_time (fixes [202012 platform_tests] TestWatchdogApi::test_remaining_time failure on vms20-t1-7050cx3-3.1 #8440 and [ 202012 platform_tests ] TestWatchdogApi::test_arm_disarm_states failure on vms20-t1-7050cx3-3.1 #8439)
Implement missing thermal infos and conditions (fixes [202012 platform_tests] test_platform_info.py::test_thermal_control_psu_absence error #8453)
Fix Chassis.set_status_led return value (fixes [2020 platform_tests] TestChassisApi::test_status_led failure on vms20-t0-7050cx3-1 #8464)
Why I did it
Update the sonic-swss submodule for the 202012 branch. The following is the new commit in the submodule.
c1cb2ca [202012] Backport SAI failure handling to 202012 branch (#1880)
How I did it
Update the sonic-swss submodule pointer for the 202012 branch.
with state of tdport from previous warm-reboot.
In case LAG was down before reboot, lacp->wr is not cleared.
In lacp_event_watch_port_flush_data we incremented nr_of_tdports and add
tdport to lacp->wr.state. In case lacp->wr.state already had this tdport
we do not set new state for tdport but appened a new item in
lacp->wr.state. In case we preformed warm-reboot and PortChannel member
was down, after reboot PortChannel member became up next warm-reboot
will initialize teamd with PortChannel member in down state.
Fix this issue by calling stop_wr_mode() when LAG was down. This was probably intended but missed.
#### Why I did it
To fix an issue seen in warm-reboot-sad test cases.
#### How I did it
I fixed it in SONiC libteam patch that adds warm-reboot support. Details in commit description.
#### How to verify it
Run warm-reboot-sad test on t0-56 topology.
ef4b3ec [Y-Cable] add the definition inside setup.py to include sonic_y_cable.credo as a package (#211)
7d81488 [Y-Cable][Credo] Credo implementation of YCable class which inherits from YCableBase required for Y-Cable API's in sonic-platform-daemons (#203)
3efb093 [sonic_y_cable] add abstract class YCableBase required for Y-cable API support for multiple vendors (#186)
Signed-off-by: vaibhav-dahiya <vdahiya@microsoft.com>
caclmgrd: monitor mux_cable_table in state_db to update dhcp acl
- if the state changes to 'standby', add acl to block dhcp packets based on ingress interfaces
- if the state changes to 'active', delete acl
- if the state changes to 'unknown', also delete acl to avoid potential disconnect
- both addition and deletion follow checking the existence of the rules
The change has been verified on a virtual switch based testbed.
Port to 202012 branch from #8222
#### Why I did it
Use a predefined variable to get vendor information when the swss docker container is created
#### How I did it
Use `{{ sonic_asic_platform }}` instead of `$SONIC_CFGGEN -y /etc/sonic/sonic_version.yml -v asic_type`
#### How to verify it
Manually test.
#### Why I did it
Create a target for delayed service timers. Few services in sonic have delayed to speed up the bring up of the system and essential services. However there is no way to track when they start. This will be a problem when executing config reload as config reload expects all services to be up. Hence grouped all the timers that trigger the delayed services under one target so that they could be tracked in 'config reload' command
#### How I did it
Created delay.target service and add created dependency on the delayed targets.
To fix failed test cases of Haliburton platform APIs that found on platform_tests script
- How I did it
- Add device/celestica/x86_64-cel_e1031-r0/platform.json
- Update functions to support python3.7
- Add more functions follow latest sonic_platform_base
- Fix the bug
Signed-off-by: Wirut Getbamrung [wgetbumr@celestica.com]
Master/202012 image size grew quite a bit. 3.7G harddrive can no longer hold one image and safely upgrade to another image. Every bit of harddrive space is precious to save now.
Also sh syntax seemingly changed, [ condition ] && action was a legit syntax in 201911 branch but it is an error when condition not met with 202012 or later images. Change the syntax to if statement to avoid the issue.
Signed-off-by: Ying Xie ying.xie@microsoft.com
Why I did it
Support to build armhf/arm64 platforms on arm based system without qemu simulator.
When building the armhf/arm64 on arm based system, it is not necessary to use qemu simulator.
How I did it
Build armhf on armhf system, or build arm64 on arm64 system, by default, qemu simulator will not be used.
When building armhf on arm64, and you have enabled armhf docker, then it will build images without simulator automatically. It is based how the docker service is run.
Docker base image change:
For amd64, change from debian:to amd64/debian:
For arm64, change from multiarch/debian-debootstrap:arm64- to arm64v8/debian:
For armhf, change from multiarch/debian-debootstrap:armhf- to arm32v7/debian:
See https://github.com/docker-library/official-images#architectures-other-than-amd64
The mapping relations:
arm32v6 --- armel
arm32v7 --- armhf
arm64v8 --- arm64
Docker image armhf deprecated info: https://hub.docker.com/r/armhf/debian, using arm32v7 instead.
Deliver sfputil support for sfputil show eeprom and sfputil reset along with some component test case fixes
Co-authored-by: Carl Keene <keene@nokia.com>
Fix#7968
Issue is detected on SONiC.20201231.11
In test_static_route.py::test_static_route_ecmp static routes are configured, but neighbors are not resolved after config reload even after 10 minutes.
It looks like the arp_update script is starting to ping when Vlan1000 is not fully configured.
When issue is reproduced, stuck ping6 process is observed in swss container :
USER PID %CPU %MEM VSZ RSS TTY STAT START TIME COMMAND
root 180 0.1 0.0 6296 1272 pts/0 S 17:03 0:03 ping6 -I Vlan1000 -n -q -i 0 -c 1 -W 0 ff02::1
And when arp_update script successfully resolves neighbors, we observe sleep 300 instead of ping process
* add hwsku.json for the Nokia-7215
* added required default_brkout_mode to hwsku as its not optional
* remove tabs from the file so spacing consistent
Co-authored-by: Carl Keene <keene@nokia.com>
Why I did it
fix the dx010 system eeprom unavailable issue
How I did it
enable the i2c slave 30ms timeout mechanism
How to verify it
i2cstress test in DX010 iSMT controller bus
Co-authored-by: nicwu-cel <nicwu@celestica.com>
enable automated test suites to selectively run relevant tests ( or not run tests ) based upon a new port_type identifier in hwsku.json
How I did it
Modified the valid optional fields in validity check for hwsku.json per recommendation from Joe in
https://github.com/Azure/sonic-mgmt/pull/2654/files
Co-authored-by: Carl Keene <keene@nokia.com>
Signed-off-by: Rajkumar Pennadam Ramamoorthy rpennadamram@marvell.com
Why I did it
Install sonic image from ONIE. Once system is up, execute "config reload" command.
Root cause is that "determine-reboot-cause.service" was in failed state.
root@sonic:/host/reboot-cause# systemctl list-units --failed
UNIT LOAD ACTIVE SUB DESCRIPTION
● determine-reboot-cause.service loaded failed failed Reboot cause determination service
How I did it
Fixed the issue by setting default reason to "REBOOT_CAUSE_UNKNOWN" instead of "None".
How to verify it
Check " determine-reboot-cause.service' loaded successfully post image installation from ONIE.
Verify "reboot-cause.txt" file is created and config reload succeeds.
Update Makefile, so it does the following:
For a given platform, verify if platform/checkout/.ini exists and
hence run the platform/checkout/template.j2. This allows platform
code to be checked out during the 'make configure' stage.